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NDRL Spring Drags

Beech Bend Raceway Park, Bowling Green, KY

May 25 – 26, 2013

We left for Bowling Green Wednesday afternoon, the 22nd of May. We hit a lot of construction, so the going was slow at times. We stopped for the night just north of Columbus. The next morning Steve was up first. He started the generator and then pressed the “on” button of the coffee pot (I always have it ready to brew). The coffee was about half done when the generator quit. Steve started it again, and the coffee pot continued for a few minutes until the generator quit again – what the hell! This has never happened before. Doesn’t that damn generator know that I NEED my coffee? Well Steve started it again and went outside to open the generator access door to see if he could figure out what was wrong. He could see that the cooling fan was not working, so the generator would overheat and shut off. This time the coffee finished by the time the generator quit. While we were having our coffee Steve got online and found an Onan dealer in Louisville. They had the fan belt for our generator in stock, so we told him we would stop on our way through to pick it up. Steve thought he would have time at the track to change the belt. When we got to the Onan dealer they told Steve that many times it was not only the belt that was the problem, but some of the fans have a plastic part that cracks. They gave Steve the info for the Onan dealer in Nashville. We were planning on leaving the whole rig in Nashville and flying home anyway, so we made arrangements for the Onan dealer in Nashville to keep the rig for the two weeks and fix whatever needed to be fixed on the generator. Now all we had to do was get thru the weekend of racing with no Motorhome generator. We would have to make do with the gas generator in the trailer, unless we could pit next to one of the few poles at the track with an electric outlet on it. Well we were one of the first to pull in, so we got that pole with the electric.

We got to the track early because we knew that an NHRA tech would be there that could do the re-cert of our chassis. He was supposed to be there all day Friday. So we got the car out of the trailer, got the body off it so that the chassis was exposed, and then we waited. We waited some more. Steve drove around in the golf cart trying to find the guy. Finally we were told that the guy would not be there until Saturday morning. So the car stayed naked all night. But the re-cert got done first thing Saturday morning. Then it went thru tech, got the body back on and got ready for the first round of qualifying.

Our run was at 11:45 am. The car left good, and the 60 ft time was good. The eighth mile time was a little fast – it was on a “breakout” run. But then Steve heard a pop. He could see a little piece of the head gasket poking out. He got out of it, but it still went thru the lights at 7.10 and 167 mph. We took it back to the pits and started taking things apart. It was not good.

The #4 main bearing had seized on the crank, causing the rod to shatter. The pictures show part of the rod coming thru the side of the block, and some of the remaining pieces of rod in the oil pan.

The cam would not turn as some of the rod was wedged in there, and there was damage to a couple of valves. So to make a long story short, that engine was toast! We did not make the call for the second qualifying run, but we still ended up #2 qualifier based on that 7.10 run

Here is where things get interesting. There was a Jegs Super Quick race at this track this weekend. And one of the racers in that event was Richard Edwards. Richard also raced with us in Nostalgia racing for years. So we knew him very well. He knew of our problem. He was there to race in the Jegs Super Quick race. He had the engine in his dragster for sale, as he had a new engine on order. He came to us and offered his engine to us. He said he would not race this weekend, but would take the engine out of his car and put it in our car. We knew that this engine would work for us so we said okay. I wrote Richard a check and we started the exchange. We got our damaged engine out, took our engine-less car to his pit to put the new engine in.

After the new engine was installed we went back to our pit where the intake, blower, starter, etc went on. All was done by 3 am. We were ready to start the car, but because this engine had a Super Mag 20, it required a 16 volt battery to start. We tried to start is with our 12 volt battery but it was a no go. At 7:00 am Richard was at our pit area with his 16 volt battery, and it started right up.

We went up for first round of eliminations. No one could believe it. We ran a 7.18 and lost to a 7.11. We have a car that can be tuned to win!!!

We will be back in two weeks for the Hot Rod Reunion, and we will be ready to compete!

Stayed Tuned.

 

Test ‘n Tune

Empire Dragway

April 27, 2013 & May 3, 2013

Over the winter Steve did some routine maintenance – new rods etc. and changed the hat to a more nostalgic “shot gun” style. And of course when you make a change it results in many other changes, such as wiring, fuel lines and so forth. So we really needed to get to the track and see what these changes did to our 2012 Pro 7.0 Champion Altered.


Photo taken by Ron Rigby

Saturday, April 27th was one of the first really nice days. Look at the picture and notice the trees – not a leaf in sight. Also, notice that new hat. We got to the track, warmed up the car, everything seemed good, and we went up for a run. Steve planned on making an eighth mile pass. First thing that went wrong was our radios would not work, so we went back to the old style where I ran down the track after the burnout to get in front of the car and guide Steve back with hand signals. Then because I couldn’t tell him told “hold it right there” until I pressed the button to start the data recorder Steve kept creeping up trying to stage the car, so I had to keep chasing after him to get to the damn button. We looked like a couple of clowns in a circus act. The car made a pretty good run. The eighth mile time was 4.54. Out eighth mile index is 4.50, so we were happy. When we got back to the pits I downloaded the data. That was the second thing that went wrong. The data recorder didn’t start recording until mid run, so I got EGT’s, some boost, fuel and oil pressure data, but no launch data or shift data. We really couldn’t figure that out but I’m thinking it was low on charge. Then we tried to go up for a second run. Steve could not get the car to stay running – it was getting way too much fuel. We took it back to the pits and tried and tried to figure out what the problem was. We started the car so many times the starter died. That did it! We packed it up and went home.

The next day Steve started to work on the car. He found that the shaft in the snout for the blower had snapped in half. So a new snout and a repaired starter, fully charged radios and data recorder and we were ready to go back to the track and try again.

Friday, May 3rd we headed back to Empire Dragway. Thankfully this was a totally different experience! This time nothing went wrong. We made two runs. One eighth mile and one full pass. The eighth mile run we ran a 4.58 and 154 mph. The quarter mile run we ran a 7.08 and 190 mph. The radios worked, the data recorder worked, and the car ran great. If we can keep this up we should have a pretty good season.

We are ready to head to our first race in Bowling Green, KY on May 25 and 26.

Stay tuned.

 

 

 

SS3 Race Team © 2008 website by jims computer service last updated 06/06/2013